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DeepFast Downhole Motor Set a Record of Longest Service Time in 8.5” Well Drilling

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DeepFast Downhole Motor Set a Record of Longest Service Time in 8.5” Well Drilling
Overview

High mud density and pump load, the adjacent well meet continuous problems due to the competitor’s PDM failure, and customer ask for long life time PDM  that at least 300 hours.

Solution

DeepFast recommend low-pressure MSS6757845-II PDM

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Performance

Satisfied customer‘s requirements, compared with conventional PDM, the pressure consumption was reduced by 2MPa, the output speed was stable, continuous working time was 417.66 hours, the footage was 2128m, and the ROP reached 9.56m/h

tptp (3)

No WELL No TYPE M.W. g/cm3 Interval/m FTG/m Circu. Time/h Drilling Time/h ROP m/h Remarks
1 WY26-4HF High temperature oil-based 2.14 3306-5236 1903 279.48 159.72 11.91 The fastest ROP
2 WY26-3HF High temperature oil-based 2.15 3312-5440 2128 417.66 222.54 9.56 The longest working time

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Total and Schlumberger highly praise DeepFast downhole motors(PDM) with an average 35% ROP increased and 0 failure

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DeepFast Downhole Motor Set Multiple Records of Zhejiang Oilfield in 8.5” Well Section

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